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Today at Atelier Kaz - ex-Honda R&D, F1, Indy/CART engineer

Updates from Kaz-kzukNA1

  1. Eng Refresh 12

    by , 12-01-2014 at 11:33 AM (Today at Atelier Kaz - ex-Honda R&D, F1, Indy/CART engineer)




    New CRK/CYL sensor installed and carefully torqued the fixing bolts.






    All four cam shafts
    ...
  2. Eng Refresh 08

    by , 04-01-2014 at 01:56 PM (Today at Atelier Kaz - ex-Honda R&D, F1, Indy/CART engineer)
    Before backing off the valve clearance adjusters, checked the
    current valve clearance.
    They were all over the place and #1 exh side were out of the spec.
    Rest of them were at the limit but within the spec.




    All four camshafts looked fine under the initial inspection with
    extra scratch marking at #3 cyl intake cam robe.
    ...
  3. Eng Refresh 11

    by , 23-10-2013 at 11:47 AM (Today at Atelier Kaz - ex-Honda R&D, F1, Indy/CART engineer)



    Another catch up updating the blog....







    The original coating of the valve cover was already contaminated
    at different level at many places.
    Also, part of the coating was already missing exposing
    ...
  4. Eng Refresh 07

    by , 13-10-2013 at 10:16 PM (Today at Atelier Kaz - ex-Honda R&D, F1, Indy/CART engineer)





    Original design WP.

    It is quite normal to see tiny amount of coolant at the drain hole over
    many years but this one looked to be already blocked.

    The bearing was nearly dead with small rattle and making squeaking noise
    when spinning by hand.



    ...
  5. Eng Refresh 06

    by , 31-08-2013 at 10:27 PM (Today at Atelier Kaz - ex-Honda R&D, F1, Indy/CART engineer)






    However, the TB tension was way too low.
    If I wanted, I could have twisted the existing TB 180deg.
    Didn't want to put too much tension so stopped at 90deg in this photo.





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