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Today at Atelier Kaz - ex-Honda R&D, F1, Indy/CART engineer

Updates from Kaz-kzukNA1

  1. Final Touch 05

    by , 23-05-2014 at 01:22 PM (Today at Atelier Kaz - ex-Honda R&D, F1, Indy/CART engineer)




    About to return this NSX to the owner so this is the final catch up updating the blog, for now.....




    I have now covered 65miles of test driving session including several VTEC moments
    and just one check of over 7,000rpm slope test.
    No issues and no warning lights, cool down mode and back on the lift.
    Visually
    ...
  2. Eng Refresh 21

    by , 05-05-2014 at 11:18 AM (Today at Atelier Kaz - ex-Honda R&D, F1, Indy/CART engineer)






    TB tensioned properly and adjuster bolt torqued to the spec.






    New TB lower cover
    ...
  3. Eng Refresh 20

    by , 05-05-2014 at 11:08 AM (Today at Atelier Kaz - ex-Honda R&D, F1, Indy/CART engineer)





    V-bank coolant pipe back in place.
    Used to look like this.








    As
    ...
  4. Eng Refresh 19

    by , 03-05-2014 at 12:15 PM (Today at Atelier Kaz - ex-Honda R&D, F1, Indy/CART engineer)





    Double checked that the brown cam seals are pushed into the correct position.
    Several years ago when I injured my back, even after visually checking the position
    of this seal, I made mistake resulting in oil seepage so since then,
    taking photos for better inspection method.



    ...
  5. Eng Refresh 08

    by , 18-04-2014 at 01:00 PM (Today at Atelier Kaz - ex-Honda R&D, F1, Indy/CART engineer)



    As always, IAT sensor was covered in sticky blowby gunk.
    Cleaned it and will be installed with new o-ring.





    ...
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